Finding The Balance

Story Image

Water is essential in the steel production process - as is the ability of steel producers to conserve and reuse water whenever possible. When one of our steel customers was facing water balance issues related to their initiative to reduce water usage, we worked together to help them solve their challenges and meet their water conservation goals.

As part of their efforts to reduce water use, the plant was recycling all of the blowdown (the water drained from cooling equipment to remove mineral buildup) from the four non-contact cooling water systems to the main process water system, which supplied cooling water for the continuous caster and rolling mill. Because the non-contact cooling water cycles were not optimized, excessive blowdown was entering the process water system, leading to the water balance issues.

Icon of a water droplet.

Using our state-of-the-art technology and service, we can help our customers with water balance and conservation.

$125,000

Our team completed an audit to understand the dynamics of the water systems, and found that poor control of the make-up and blowdown valves was leading to excess fresh water make-up use. And the existing treatment program had increased stress on the cooling towers, causing corrosion, iron deposits and water losses. Our team installed 3D TRASAR™ technology on four open, recirculating cooling systems to detect changes in water chemistry and determine corrective action needed. Combined with our Ecolab Global Intelligence Center, this solution helped stabilize our customer's balance issues while helping them reduce their water usage.

  • Water savings of 60 million gallons of water a year
  • Water consumption per ton of steel reduced by nearly 30%
  • Cost savings of $125,000 annually

Related Success Stories

Partnering with customers to solve their greatest challenges.

Nalco Water RRA™ Technology Helps Alumina Customer Save Water and Improve Profitability

Nalco Water introduced a proprietary emulsion flocculant, called RRA™, to enhance the handling of red mud tailings. ...

Amine Performance Provides Gas Plant Real-time Information Results in Operational Efficiency Improvements

Nalco Water’s OMNI Amine Performance Monitor was installed to help determine the reason for this plant’s high usage. One...

This partnership is the whole package

Nalco Water implemented 3D TRASAR™ Water Management Technology to help the turbine condenser operate more efficiently. A...

West Coast Refinery Reduces Water Consumption in Drought-Stricken Region

Using its Best Practices Gap Analysis, Nalco Water identified the refinery’s boiler system as a potential reliability ri...

Water Savings for ADM Ethanol Facility

Ecolab’s CIP technology and associated chemistries led to more consistent fermentation and enhanced system performance a...

Using Digital Insights to Help Reduce Hospital Infection Rates

Proper hand hygiene helps everyone stay healthy in daily life....

New 3D TRASAR™ Technology for Desalter Brine Improves System Assurance and Helps Optimize Tramp Amine Removal

Robust monitoring & control achieves consistent performance without compromising asset reliability. ...

Innovative Field Test Allows Refiner to Manage Risks Posed by Crudes Contaminated with Tramp Amines

PATHFINDER™ Amine Test provides an added layer of protection from tramp amines....

Best Practices for Tramp Amine Contaminated Crude Improves Crude Flexibility

Providing crude flexibility while mitigating tramp amine risks. XX Discountinued...

How 3DTRASAR for Pulp Wash Delivers Consistently Clean Pulp

Discover how data driven 3DTRASAR for Pulp Wash improves washing performance, supports process consistency, and helps mi...

Helping Save Water and Improve Operations in Texas

Austin, Texas plant produces chips that go into mobile devices. Ecolab 3D TRASAR™ Technology has helped the plant dramat...

Wrapping Up Savings in Papermaking

Read how a pulp and paper company implemented PARETO Mixing Technology to save $95,000 per year....